High Pressure Fan Prototyoing


 

High Pressure Fan Prototype

 

Older fan has proven insufficient for task.

 

 

Goals:

 

 

 

Reasearch Notes:

 

     Modeling the fan after various concepts from Cincinnati Blower.

 

 

Version 1:

 

Modeled in SolidWorks 2010. CNC Plasma Cut.

 

 

     After a serious round of figuring out the simplest means by which to seal the fan. I pretty much threw out most of the rubber/silcone gaskets as impractical. Also due to thier close to failure temperature ranges, and installation pain. So I Decieded to try FOIL aluminum tape. Bingo. Worked great. In fact this worked so well, we are going to pursue more options within that idea. Copper Beryllium tape would be ideal as the coefficient of expansion is roughly the same as steel. But I'd be happy with close enough. 

 

We ran two tests of this, both with our 12vdc Fan motor (cheap/low cost) and the same cowling and test set up. The only difference was the rotor size. We maintained the blade to rotor ratio DIA, and kept the blade at the same width. 0.7"

Our first test we ran with a rotor of 10"DIA. The Second with a rotor of 11.5"DIA. Note the ID of the blades stayed the same on both rotors. Close to the hub as pictured. The OD followed the rotor diameter.

Here are the results. (in brief) Again note that this a 12VDC fan-motor, the rpm drops under load. And note that the decreasing rpm in each test refer to a different motor speed wire.

 

Fan Results: 

Static test, 4" intake blocked at 5" depth.

 

10" rotor 12" cowling 0.7inch blade

Battery @13v with addition of charger. (to maintain charge and current)

 

4200rpm = 8.75inches/h2o   orange wire  -high power

3150rpm = 5      "                   red wire       -med power

2200rpm = 2.75     "               yellow          - low power

 

11.5" rotor with same cowling set up and batt/charge.

 

3500rpm = 8.3 "

2641rpm = 4.7 "

1796rpm = 2.3 "

 

 

The next design we should be able to achieve the 10"/H20 mark that we have set out to do.